4C and 11D Failure Analysis of Helium Pressure Regulator (Fuel Tank) DWR. NO. 27-08217-3
Abstract
This test was conducted to analyze failures that occurred in the airborne pressurization system of missiles 4C and 11D. The objective of the test was to determine if heating of the motor section pressure/bleed line on the regulator would result in a condition similar to that which caused the failures.
Document Details
- Document Type
- Technical Report
- Publication Date
- Aug 11, 1960
- Accession Number
- AD0842100
Entities
People
- D. J. Melvin
Organizations
- General Dynamics