Production Quality Assurance Testing of a Thiokol Minuteman LGM-30G Stage 3 Rocket Motor at Simulated Pressure Altitude, Motor PQA-102

Abstract

An LGM-30G Stage III solid-propellant rocket motor, PQA-102, was fired in Rocket Development Test Cell (J-5), Engine Test Facility (ETF). The roll control subsystem was independently tested off-motor. Motor ballistic, roll control system, thrust vector control, and thrust termination system performance was within model specification requirements. The motor was ignited at a pressure altitude of 102,000 ft. Motor ignition delay time was 86 msec. Motor thrust termination occurred at 60.18 sec at a chamber pressure of 75.3 psia. Motor action time was 60.18 during which the motor produced an unaugmented vacuum total impulse of 2,083,534 lbf-sec. The unaugmented vacuum specific impulse was 284.94 lbf-sec/lbm. The roll control subsystem structural integrity was satisfactory.

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Document Details

Document Type
Technical Report
Publication Date
Apr 01, 1973
Accession Number
AD0909395

Entities

People

  • C. H. Kunz
  • D. E. Franklin

Organizations

  • Arnold Engineering Development Complex

Tags

Communities of Interest

  • Weapons Technologies

DTIC Thesaurus Topics

  • Air Force
  • Control Systems
  • Engineering
  • Ignition
  • Ignition Lag
  • Intercontinental Ballistic Missiles
  • Measurement
  • Production
  • Propellant Grains
  • Propellants
  • Recording Systems
  • Rocket Engines
  • Solid Propellants
  • Specific Impulse
  • Strain Gages
  • Test And Evaluation
  • Test Facilities

Fields of Study

  • Physics

Readers

  • Rocket Propulsion.