Preliminary Airworthiness Evaluation AH-1S(Prod) Helicopter Equipped with a Substitute Straight Exhaust Pipe.
Abstract
A limited performance and handling qualities evaluation and an engine and transmission cooling survey of an AH-1S (PROD) Helicopter equipped with a substitute straight exhaust pipe was performed at Edwards Air Force Base between 20 and 23 August 1979. A total of 8 hours, 6.3 of which were productive, was required. No significant changes in performance or handling qualities were found as a result of the substitute straight exhaust pipe installation. The engine and transmission cooling characteristics were similar to those of a production AH-1S and were satisfactory. No previously unreported shortcomings or deficiencies were identified. (Author)
Document Details
- Document Type
- Technical Report
- Publication Date
- Jun 01, 1980
- Accession Number
- ADA092614
Entities
People
- Charles E. Frankenberger Jr.
- John Niemann
- Patrick M. Morris
- Ralph Woratschek