Applegate Dam Spillway and Outlet Works, Applegate River, Oregon. Hydraulic Model Investigation.
Abstract
The Applegate Dam project, located in southwestern Oregon, provides flood control storage and includes facilities for upstream fish migration and temperature control of normal project releases. This report presents the results of hydraulic model studies used in the final design of the project spillway and flood control outlet. Tests with the spillway model indicated that the originally designed approach channel invert could be raised 20 feet and still maintain satisfactory spillway operation. The reduction in approach-channel depth resulted in a considerable decrease in excavation costs. The model was used to evaluate the performance of the spillway plunge pool. Initial operation of the outlet model revealed the existence of an unacceptable roostertail emanating from the nose of the splitter wall separating the two outlet entrances. The model was used to develop a pier modification which reduced the roostertail to acceptable limits. The report also presents test results used in evaluating performance of the outlet works stilling basin which consists of a unique, dual-chamber hydraulic-jump basin stilling basin which consists of a unique, dual-chamber hydraulic-jump basin which also functions as an entrance pool for the fish passage facility.
Document Details
- Document Type
- Technical Report
- Publication Date
- Sep 01, 1984
- Accession Number
- ADA147010
Entities
People
- M. M. Kubo
- Robert L. Johnson
Organizations
- United States Army Corps of Engineers