AH-1S(MC) Degraded Hydraulics Mode Evaluation

Abstract

In a limited evaluation to assess degraded hydraulic system collective control limiting of the AH-1S(MC) helicopter equipped with K747 main rotor blades, conducted by the US Army Aviation Engineering Flight Activity (USAAEFA). Testing was conducted at Edwards Air Force Base, California between 5 October and 14 October 1985. Twelve flights were flown totalling 9.5 hours, of which 7.9 hours were productive. One deficiency was identified: the collective control limiting after a hydraulic system failure which if experienced in an out-of-ground effect hover may result in a mishap. Collective control limiting occurred when the minimum value of the collective actuator load reached 1050 + or - pounds. The maintenance test flight (MTF) procedure which was evaluated was unsatisfactory. A recommended MTF procedure, developed during this test, is included.

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Document Details

Document Type
Technical Report
Publication Date
Jan 01, 1986
Accession Number
ADA178764

Entities

People

  • Austin R. Omlie
  • Patrick J. Sullivan
  • Richard Adler

Tags

Communities of Interest

  • Air Platforms
  • Weapons Technologies

DTIC Thesaurus Topics

  • Air Force
  • Air Force Facilities
  • Aircraft Equipment
  • Aircrafts
  • Airfoils
  • Airframes
  • Altitude
  • Army Aviation
  • Axial Loads
  • Control Systems
  • Control Systems Engineering
  • Engineering
  • Helicopters
  • Hydraulic Tests
  • Radar Altimeters
  • Test And Evaluation
  • Turboshaft Engines

Readers

  • Aerospace Engineering