Test Report XB-70A Flight 1-14
Abstract
The fourteenth flight (1-14) of the XB-70, No. 62-001, aircraft was successfully completed on 1 July 1965. This same mission was aborted after lining up on the runway the previous day because of a problem with a landing gear wheel spider. Programmed tests were conducted and apparent improved performance resulted from a new climb schedule and from operating the inlet at higher recovery positions. After landing, two areas of honeycomb face sheet were found to be missing along with other face sheet separations. This flight was completed in accordance with the test plan. Improved performance was seen as a result of a new climb schedule and operating the duct at higher recovery positions. Maximum speed and altitude were Mach 2.85, 585 KIAS, 68,000 feet. Maximum indicated total temperature observe by the flight crew was 508 deg F.
Document Details
- Document Type
- Technical Report
- Publication Date
- Jul 01, 1965
- Accession Number
- AD1169070
Entities
People
- Guy M. Townsend
- Ira L. Plummer
- Joseph F. Cotton